posted by 2fass240us on Aug 19
After getting back in town Sunday and losing 4 valuable days in my build, I decided that I would take the first half of Monday to run a few errands. I took the two lines I bought from raceprovenparts, an eBay store, to BMRS where they were originally manufactured to have them altered. At $19 each plus $10 for shipping, they were a steal. I had 3 lines made out of them:
- Oil block to check valve (then filter canister); straight into 90°
- Filter canister to oil cooler: straight into 45°
- Oil cooler to oil block: 90° to straight
I spent $85 on two straight and two 90° fittings, which most enthusiasts would say is too much. But the price includes the labor to crimp them on and pressure-testing the lines to 375psi to make sure everything works as designed. Considering the lines were used, I think I came out way on top. I have four feet plus of high-quality Nomex, -10 lines with world-class fittings for $135.
I test-fitted the lines when I got back home, giddy as a boy on Christmas morning. Line #1 was a little long and had a vertical hump if attached straight, but I turned the 90° fitting a little and now the line kinks slightly to the left. The line from the oil cooler back to the block was longer than I really needed, so I routed it between the check valve and wheel well and covered it with a piece of rubber hose and zip ties. I could’ve taken the line back and had it shortened, but then I’d have to pay for the new straight fitting at $16 plus the gas to and from, plus the time to do it. This way the run becomes a little longer, but gives the check valve some support and moves the line out of the way of other components. It also looks nicer despite the rubber hose piece. The line from the canister to the oil cooler was by far the easiest.
When attached aluminum fittings to aluminum fittings, it’s always a good idea to use some Anti Sieze to keep the threads from galling. Apply lightly and run it down a time or two to get all the threads covered, and you’re good to go. Tighten them by running them hand-tight, then turning 1/4 turn more with a wrench. Some of mine were difficult to attach, and it turns out it was from water in the fittings from the pressure test. Make sure you remove this, as it’s far from being the best lubricant.
After getting everything in place, I filled the oil cooler by pouring oil in the element-less filter canister and letting it run down the line to the cooler. I then put the filter element back in, tightened the cover, and cleaned the Anti Sieze off the fittings.
The oil pressure sender caused even more headache than I thought it might. After getting some BSP:NPT fittings in my BAT Inc. order, I thought I had it licked. Not only was the oil block not BSP, but I really can’t figure out what thread it is. I took the old brass fitting used with the OE oil block to four places yesterday morning, and was none the better for my wasted time and gas. The block end appears to be metric, 10×1.25, but even that was uncertain. So as much as I didn’t want to, I reused the brass one because I thought it a better alternative than pulling my dash to re-route the sender wiring, and having the sender hang off the oil block. For the latter, it is generally believed that this has led to sender failure from vibration, and I have no desire to replace the $120 sender. Hindsight being 20/20, I would’ve gone with a used NASCAR Stewart Warner gauge or a new Autometer. It will be especially silly when I eventually put an LS1 in and have metric gauges, but I could likely sell them for a profit.
I decided to test the system for leaks because it’s laborious to put the intake manifold back on. I filled the engine up with oil and checked the level, then hooked up the battery. I turned the key partway, then heard a fluid spilling sound. Apparently, it’s a good idea to pull the fuel pump fuse when you have open fuel lines and want to turn the car over. I cleaned that up, cursing myself, and pulled the fuse. After 7-8 times turning the engine over, I was unable to build oil pressure. I looked for leaks, and realized that I hadn’t tightened the drain plug. I was on a roll!
I didn’t try again, but think the culprit might be the open connector on the valve cover that connects to the fuel rail. I will cap it off and try again, but it might simply be a matter of turning the engine over a lot. If this is the case, I might borrow the battery from the Pathfinder as the little Odyssey gets worn out quickly from when the engine was first fired up. I’ll also get someone to help me by opening the fill cap and making sure oil is coming out of the cam squirters. It’s probably something small, as no engine work was done and the oil pump should be working without issue.